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579th STRATEGIC MISSILE SQUADRON WALKER AFB SITE 5 ACCIDENT FEBRUARY 13, 1964
January 12, 1999 I
am writing this account of my recollections for the purpose of providing this
information to anyone who wishes to use it.
I recognize that it may not be readily understood by those who are not
already initiated into the weapon system, but who else would be interested,
anyway. I would be happy to
communicate with anyone who has interest in or would like more information about
the incident which I describe herein. My
address is: Allan L. Kane 6609 S.E. 160th St. Olalla, WA 98359
AKane42533@aol.com With
the draft breathing down my neck, I enlisted in the Air Force on Dec. 14, 1961
and, following Basic Training, was assigned to Shepard AFB and attended the
missile training school there. Following this I went to Walker AFB, arriving in Oct. 1962.
I was assigned to Crew #60 and we traveled to VANDENBERG AFB in April,
1963 for our operational training. Shortly
after our return to Walker my crew was deemed to be adequately qualified and we
began regular duty rotation at the various complexes. I
have very little in the way of documentation and the majority of what I write is
based upon recollections alone, and not hard data or documents.
The only things I have are my note made just prior to leaving the Launch
Control Center following the incident which destroyed the silo.
On this scrap of paper I wrote the number 61-2475 which no longer has any
meaning to me. It may identify the
installation and I must have considered it to be something of significance to
that particular site. I also wrote
SM-65F, which is the military designation for the Atlas F weapon system,
13 Feb. 64, which is the date of the incident, 11:10:22, which is the time of
day at which the clock in the LCC stopped, R-60, which was our crew number and
Capt. V.P., Ford, Jr., the Crew Commander.
I also have some artifacts from the site which I picked up as I left the
site that day and which I collected during subsequent trips to the site.
These artifacts consist of pieces of the missile skin, hydraulic system
components (fittings, valve handles, component ID tags), an elapsed time clock
powered by 400 cycle source (probably from a guidance system component or the
400CPS generator), the launcher platform ID plate, an ID plate from a
Worthington compressor and a piece of steel decking plate (probably part of the
launcher platform). It
was generally known, prior to the actual date of the test, that there would be a
PLX at our site in the near future, but neither I nor other crew member knew
when it would occur. It was clear that our site had been chosen, as the
operational warhead had been replaced with a dummy unit, the engine ignitors had
been replaced with the fuse block and other typical preparatory activities had
been accomplished during the days preceding the test. As I recall, we were notified at our pre-departure briefing
of the intent to initiate the PLX during our tour, but I am not certain of this.
It was clear, however, as soon as we arrived at the site that the PLX was
scheduled for our tour. There were
a number of extra people at the site, or they arrived shortly after we did, who
were obviously there to observe the event.
I recall that our Sector Commander was there, along with others of the
rank of Colonel and below. As I
recall, we relieved Major Goons crew that day and I recall some of his crew
members expressing relief that they had not drawn the short straw. Our crew composition on that day was as follows: MCCC - Capt. Vincent Paul Ford, Jr. DMCCC - 1LT Howard Jones BMAT - SSGT William Jenkins MFT - A2C Allan L. Kane
EPPT - A2C (or A1C) Wayne Egnew I
remember being in the vicinity of the LCC prior to the initiation of the
countdown, with all crew members present. Capt.
Ford and Lt. Jones were discussing the procedure and how they felt about it.
Ford offered that he was as nervous as a f---ing cat
He remembered shortly after having said this that all conversations were
being recorded and was sincerely mortified.
He generally tended to be of a nervous temperament, and he clearly was
now. This is not intended as a
criticism, as we were all pretty apprehensive about what we were about to do.
He just exhibited his apprehension to the tape. We
received the message from the airborne command post and the MCCC and DMCCC
authenticated the message. I recall that the call name for one of the command posts was
Looking Glass, but am not sure that the order came from this unit.
At the defined time, the MCCC initiated the countdown and began the
sequence. The countdown progressed
normally through the initial phase with no malfunction or indication of anything
out of the ordinary. It went as
smoothly as one of the many tests we had run in the past using the Launch Signal
Responders. Following
the successful completion of the initial phase of the countdown, the DMCCC took
his key and moved to level 1 and to the Commit station at that level.
The MCCC gave the order to Commit on my mark-MARK, and turned his
key. The DMCCC obviously turned his
key within the allotted time and we began the commit phase. The activities during this phase, as I recall, included final
topping of the fuel and LOX tanks, guidance system checks and final setup and
transferring of systems to internal control.
The initial phase of the commit sequence proceeded normally up to the
point at which the launcher platform began its ascent to the surface.
One of my responsibilities was to monitor certain areas within the silo
during countdown by use of closed circuit TV units.
One of the cameras was installed in the missile enclosure area and
provided a view from the bottom of the silo toward the underside of the launcher
platform after it moved from its lowered position.
As the launcher platform rose in the enclosure, I noticed a liquid
cascading from the platform and falling into the silo.
I notified the MCCC of this and informed him that this was not normal and
that it was evidence of a problem. He
acknowledged that he understood and that he would keep the missile at the cap by
withholding the initiation of the Abort sequence after reaching the up and
locked position. Normally, after
reaching the up and locked position during a test the Commander would initiate
the Abort sequence to cause the missile to lower into the silo, download the
oxidizer back to the silo storage tanks and return the system to a stable
condition. It
appeared that the liquid which I had observed was fuel, since the only things it
could reasonably be were fuel or hydraulic fluid and it appeared to be less
viscous than hydraulic fluid. We clearly had a problem which demanded an investigation
before we lowered the missile back to a standby position. Because of the high probability that the fluid was of
hydrocarbon nature (whether fuel or hydraulic fluid) and that, because of the
location of the plumbing which conveys the oxidizer, it was likely that this
plumbing had become contaminated. Transfer
of the oxidizer through the contaminated system would be an invitation to
disaster. We all knew that the
mixing of hydrocarbon and liquid oxygen produces a gel material which is very
sensitive to shock and will explode with very little provocation.
The only way to transfer the oxidizer from the missile to the silo tanks
was through this plumbing and we were unwilling to do this unless we were
certain that the system was clean. The
EPPT and I were the ones with responsibility to investigate situations of this
nature in the silo. The commander directed us to don our emergency gear and to
proceed into the silo to see what the conditions were.
Neither of us were enthusiastic about this, as the location to which we
must go was at the lower levels of the silo, inside the missile enclosure, and
we would have to use the stairway to both get down and to return.
It would not be safe to use the personnel elevator with the potential for
explosive gases in the silo, as the controls for this unit contained open relays
which caused arcing during normal operation.
These relays were, incidentally, quite troublesome at some site.
The contacts tended to burn and weld, disabling the elevator. At
this time, one of the upper level officers (Colonel),an observer at the event,
directed that the Non-Essential Motor Control Center be opened.
The idea was that doing this would deactivate all of the non explosion
proof receptacles in the silo. This
would decrease the probability of ignition resulting from arcing within these
fixtures. There are a number of other circuits which are controlled by
this MCC, including the silo air handling equipment. None of us recognized the full significance of this action
and it did seem reasonable to deactivate the open receptacles.
I should add here that the situation which we were experiencing was not
one covered by any existing emergency condition checklist, and we were making
some of the procedures up as we went along. Wayne
and I prepared to enter the silo dressed in our asbestos suits and wearing our
Scott Air Packs. Thus equipped, we had some difficulty maneuvering and I
recall wondering how we would be able to make our way down and up the spiral
staircase. Nevertheless, we
proceeded through the first blast door (known as the debris door) and shut it
behind us. We moved down the tunnel
and had nearly reached the second door (this is the thick one) when the lights
began to dim. The generator was
slowing - obviously not a normal situation.
Wayne and I returned to the LCC, as he was the one who would have to
start the other generator and put it on line.
We had operated both generators in parallel during the countdown, as both
were required for a tactical launch. (I
think we could actually get the launcher platform up with just one unit, but we
used both for the PLX) Wayne
started the other engine and during this time the operational unit began to pick
up speed. He paralleled the unit
and shut down the faulty unit. At
some point we heard what sounded like a muffled boom from the direction of the
silo. I dont recall the actual
sequence, but it could have occurred during our move through the tunnel. After
having restored power neither Wayne nor I was willing to proceed into the silo.
There was clearly something serious happening there and we both knew that
entering the silo would likely be the last thing either of us did. Fortunately, the commander recognized this and did not direct
us to do so. During
this time there were at least two maintenance personnel involved in connecting
the missile tank pressurization unit to the missile.
This was a unit located on the cap, intended to provide the control
required to maintain proper pressures in the fuel and oxidizer tanks during the
extended stay on the cap. This was
a normal procedure for a situation in which a missile must remain up and locked
for an extended period of time. The
two maintenance men were up on the L/P making the connections and I was viewing
their activities by means of my cap mounted camera when I saw liquid oxygen
begin to gush from the main fill and drain line.
This line runs up the side of the missile from the vicinity of the engine
skirt to a point above the intermediate bulkhead, where it enters the oxidizer
tank. As I recall the line is
approximately 8 inches in diameter, and could have been larger. The line was flowing full and, if it continued to flow, would
dump the entire load of liquid oxygen from the missile tank in a very short
period of time. When the
maintenance people realized what was happening, they both climbed down from
their positions on the platform and fled the scene.
One took the truck, an International Crew cab, and the other ran for the
main gate. I recall the one running
made it to the gate before the one in the truck.
At the time it made quite an impression on me, but the distance was not
that great and the driver lost quite a lot of time getting to the truck and
getting it started. Shortly
after this, I lost sight of anything on the cap.
The cloud of oxygen enveloped the camera and most everything else on the
cap. The
oxygen spread out around the cap and quite a lot of it must have flowed into the
silo, as well. I am sure that a lot
of it must have entered the silo in a liquid state, although I have no evidence
to support this. Shortly
after this we all heard a fairly large boom, more intense than the first one,
and we lost power in the LCC. We
could do nothing but wait from that point on.
I recall that as I was moving around the LCC I backed into one of the
support structures of the LCC and my Air Pack banged against it making quite a
loud noise. This caused most of those present to jump and to express
great relief when it became clear that the noise had come from a source other
than another explosion. During
this time someone in the silo was in contact with a person, via land line, who
was stationed on a hill some distance from the site.
As I learned later, this person was providing information as to what was
visible from his vantage point and which we would not otherwise have known.
He stated that there was a fire directly under the missile and that there
was smoke issuing from the silo. He
also said that at the time of the actual destruction of the missile, the warhead
rotated 180 degrees and fell through the body of the missile. I
dont recall how long it took for the cap area to reach a condition allowing
our escape from the LCC, but it was probably not longer than a half hour.
The major action subsided relatively quickly, and the topside observer
provided us with the information that the condition was safe for exit.
It seems that we had some trouble in getting through the security area on
our way out, but I am not sure. In
any event we went up the stairway and out into the light.
We had been cautioned to not touch anything as we left the complex,
probably to preserve all evidence as it existed.
I ignored this directive and picked up some things as I walked toward the
gate. Others may have, as well, but
I dont know. I
cannot recall whether we were taken back to the base in separate vehicles or
not, but after arriving we were put in separate rooms and questioned
individually. This went on for
about an hour, as I recall, possibly longer. There were subsequent sessions during which we were asked to
describe the event, and at one such session, there was a legal representative in
presence. One area of questioning
had to do with training and whether our crew had experienced all of the required
instruction and testing. One of the
training activities about which they had questions was one which was crew
administered - the MCCC presented some information and was to have certified as
to our participation. I dont
recall the subject of the training, but failure to have properly performed it
could have reflected poorly on the MCCC. I had reason to believe that something about our training
session had not been entirely by the book and I refused to answer the questions.
This caused some consternation on the part of the investigators,
particularly when the attorney advised them that I did not have to respond and
that they could not demand that I tell them why I would not respond.
After some discussion and following their assurance that they were not
out to hang Capt. Ford, I did answer their questions.
My comments apparently did not cause him any harm, as he was promoted to
Major shortly after the incident. I
am not aware of any formal, official statement regarding the actual cause of the
destruction of the complex, but there were unofficial speculations as to what
actually happened. I will detail
that as well as I recall. The
fundamental cause of the incident was that the drain sequence for the fuel
system did not occur as it should have. This
sequence is intended to drain all of the fuel in the lines above the disconnect
fittings on the launcher platform. These
line are full during Commit to provide for continuous topping of the on-board
fuel tank up to the time the L/P begins to rise. The
drain sequence takes place during Commit, just before the L/P begins its ascent. The
residual fuel in the L/P lines drained out after they disconnected from the
fixed portion of the fuel system. This
was what I observed falling in the enclosure. The
speculation is that the fuel vapors were drawn into the silo main air handling
exhaust plenum located on Level 2, just at the end of the tunnel.
When the Non Essential MCC was tripped the fan in this plenum stopped
running and allowed the gases to reach an explosive level.
Something caused the vapor to ignite and the plenum disintegrated and
sent shrapnel flying around Level 2. All
of the electrical wiring which connects the silo with the LCC passes close to
the plenum as it enters the tunnel. Some
of the flying debris cut into the wiring harnesses and produced the signal which
caused the main fill and drain valve on the missile to open.
Once this happened there was no chance to save the site. I
have heard speculation to the effect that the fires under the missile, on the
L/P, could have caused the ignitors in engine supply turbines to cook off.
Since the fuel and oxidizer supply lines to the turbines would have been
closed in preparation for the PLX, the turbines would spin without the
resistance provided by the liquid. They
disintegrated and sent particles of debris up through the tanks, causing their
collapse. There was a report from
the topside observer that there was a fire burning on the L/P just below the
missile. This would support the
theory of cook off. I
cannot explain the generator malfunction. It
is possible that the quality of the intake air caused an upset in the combustion
mixture. Whether that would produce the situation which we experienced
or not, I dont know. I
have considered attempting to secure the official record of the investigation
from the Federal Govt. through a Freedom Of Information action.
I have not done so, but it seems that the files on this incident should
have been declassified by now. Following
this incident, the AF issued a revision to the manual describing the PLX
procedure which required that the liquid oxygen be replaced with liquid nitrogen
in the silo oxidizer storage tanks as a normal procedure in preparation for a
PLX. This may have occurred
following the next loss. I think
one of the losses occurred after this one, but I am not sure.
In any event, the losses caused the AF to rethink the PLX procedure and
conclude that using liquid oxygen in the procedure presented more hazard than it
was worth. I do not recall that our crew had any extended time away from duty, but I suspect that we did. We resumed duty at some point and continued in a normal rotation throughout the remainder of the life of the system.
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